Vintage Schematic Mistakes

Every once in a while, you run into places where a drafting tech made some mistakes on the schematics. This one was a Philco 42-360 radio, which has the wrong tube called out in the tube line-up vs. the schematic.

The actual radio uses an 84/6Z4 rectifier tube, but the tube line-up shows a 5Y4 in its place. These would definitely not work if substituted.

It’s pretty common to find drafting mistakes. Another Philco, wired per the schematic, had no B+ on the detector/1st AF tube. The Sam’s Photofact of the EICO HF-81 has the tubes all numbered wrong, versus the EICO schematic where they’re correct. And so on.

Keep a close eye out when working on vintage gear! You can’t always trust the schematics.

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Harman/Kardon Control Amplifier A-401 Restoration

This little Harman/Kardon Control Amplifier, model A-401, just came through the shop for a full overhaul. It was in a pretty sorry state to begin with – one channel distorted, one barely gasping for air, and a world of scratchy controls in general need of attention. Despite the electrical shape, though, it was in great cosmetic condition and definitely worth a full rebuild.

Physically, it’s a very unassuming piece of gear with elegantly understated styling, the height of ’70s simplicity. Featuring up to 20W output per channel with low distortion, it’s a great small desktop amp or perfect for pairing with a vintage hi-fi system and will fit in with nearly any decor. No wonder the owner wanted it fixed up!

The inside was untouched, which is always nice to see. It’s a very open, accessible construction design. All of the PCBs could be accessed by removing the top and bottom covers without removing any boards from the chassis itself, and every component was easily accessible. After 40+ years, the original 2SC1030 transistors had tarnished pretty significantly but otherwise everything was in decent cosmetic shape.

For whatever reason, this amp had two tantalum electrolytic capacitors – the blue components on the right of the vertical board – but the rest were all standard aluminum electrolytics. I set out for the component replacement which was very straightforward. As expected, the caps were failing and had started to leave some residue on the boards.

All the electrolytic and tantalum capacitors in this amp were replaced with Nichicon Fine Gold audiophile grade electrolytic capacitors. These are much better components than anything that was available at the time and really help to bring out the best in these vintage amps.

Finding drop-in replacement capacitors is pretty tough, but I got lucky with these. Left, the original 6800 uF 35V capacitors, and right, a pin-compatible drop-in replacement of 6800 uF at 100V. Easy! Running massively de-rated like it is, and with the advantages of modern construction techniques, these main filters will almost certainly last decades. It’s always possible to make modifications to use whatever capacitors are available, and sometimes it’s unavoidable (10 mm-spacing screw terminal radial capacitors come to mind)  but it’s much easier, and cleaner, when there’s a drop-in replacement available. This amp could take up to about a 10000 uF capacitor in that position and still be within tolerances, so there’s some flexibility.

Even after all these repairs, it sounded fantastic – from one channel. The other channel was cutting out intermittently and had hum and distortion. While probing, the amp blew both its power supply fuses. It turns out that one of the mica insulators under the output transistors was damaged and wasn’t insulating very well; there was a conductive path to the heat sink. These transistors were pretty worn, anyway, so the owner approved a minor upgrade to a modern, new manufacture TO-3 output transistor with much improved ratings – the MJ15003.

During the troubleshooting process, I did identify the defective 2SC945 transistor in that channel’s driver circuit which was causing some distortion. It was a part of a push-pull pair, but only delivered about 1/10th the gain as its compliment on the other side, thus causing the distortion. Replacing it cleaned up the worst of it, but the channel was still popping and snapping a bit for several minutes after powering on. A quick check of the driver transistors in that channel found a few that were weak, intermittently conducting, and poorly matched – so they got replaced, too.

That took care of the problem!

After replacing the parts, everything checked out! It was time to adjust the bias to ensure it’d be a safe operation, then on to performance characterization.

I was very impressed with the results of the tests. This amplifier was flat +/- 0.3 dB  through my distortion analyzer’s signal generator range, 10 Hz – 20 kHz. The MJ15003 is also much more capable than this amplifier is asking of it so there’s quite a lot of headroom, and the more efficient signal path due to the up-rated components plus more powerful output transistors resulted in 50% more measured power output at very low distortion.

At 1 kHz, THD was below 0.1% through most of its original power rating of 20%, beating its specification by 67%. This one, however, was able to deliver 30W with a 150 mV input at maximum volume, still with a THD below 0.5%. That’s audible to many ears but still listenable for the few times you might really need the extra power.

This was a fun project, and it’s going to be a great little amp for a desk or an apartment for a long time.

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EICO Stereophonic Integrated Amplifier HF-81 Repair

From the late ’50s, I had this nice example of an EICO HF-81 amplifier come through my shop. These are nice little stereo amplifiers with a built-in phono pre-amp and RIAA equalization and feature about 14W of power output per channel from a pair of push-pull EL84s each at about 1% distortion.

EICO was a popular brand of electronics kit maker back in the day. They made a lot of hobbyist or entry level shop test equipment (oscilloscopes, generators and testers) but had a handful of hi-fi stereo kits as hi-fi listening grew more and more popular. The fact they were assembled as kits makes them pretty straightforward to service, too – the layout is clean and there’s a lot of room on the chassis. It had been worked on a few times in the past – several coupling capacitors were replaced with early film caps in what looks to be the late ’60s/early ’70s. Just recently, the owner reported it was giving noise from one channel and took it to another local shop where the technician replaced a 50 uF capacitor (orange, bottom left) with a 100 uF cap that looks to me like it was probably an old-stock capacitor (blue, bottom left.) They’d clipped the old cap out of circuit but left its shell intact; not exactly what I’d call a best practice. More problems started cropping up shortly thereafter as the rest of the original capacitors degraded, so it came to me for an overhaul. After replacing the parts, there was still noise,  distortion, and lower volume on one channel seen on the oscilloscope screen in yellow. Tracing through the circuit, it turns out the CRL couplets in the tone network were failing.

I fabricated new PCBs with the same values to replace the damaged parts and mounted them to the shield.

That fixed the problem right up! After some final tweaks and a burn-in test, she’s ready to go home. Lots of parts out of this one:

It’s going to sound great for years to come!

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Boes 901 Series IV Active Equalizer #241792 Refurbishment

Bose® 901 Series IV Active Equalizers are getting up there in years now, too, so more and more are coming up for repair. This one came in with a flickering power supply in need of an overhaul.

Series IV was the first model to switch over to using op-amp ICs instead of discrete transistors for each gain stage, and used higher quality film capacitors that don’t degrade like the dipped mylar ones on the earliest Series I and Series II equalizers. Depending where in the production run you are, these might be soldered or socketed, RC4558s or TL072s. Bose specified both interchangably.

These early op-amps do start to go bad and get noisy, so they’re replaced as a matter of course along with the electrolytic capacitors. In this case, they’re soldered in, but nothing the desoldering tool can’t take care of.

This one is getting all new capacitors, including audiophile grade film capacitors for the final output caps to minimize distortion and increase clarity. The rest of the caps were all replaced with Nichicon Fine Gold audiophile electrolytic caps, too, so this is a major upgrade in capacitor quality.

New Texas Instruments TL072P chips to replace the old, noisy ones.

In conclusion, this one cleaned up very nicely. Most Series IV and earlier Active Equalizers could benefit from service these days due to their age, this one received major upgrades and should sound much cleaner even than when it was new.

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Vintage Engineering is Beautiful

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EL84 output tubes in an EICO HF-81 integrated stereo amplifier.

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Marantz 2270 Stereophonic Receiver Overhaul

I just had a great stereo receiver through the shop for repairs, the Marantz 2270. It’s the big brother to the Marantz 2245 I had through the shop a little while ago – mostly the same front-end circuitry, but with the addition on a multipath indicator to the FM tuner, and of course different final amplifiers.

This is a very early example, serial #3593 from the beginning of the production run. It was designed in the USA and manufactured in Japan.

These receivers were really built incredibly well. They’re easy to work on, for the most part, and delivers a lot of power with very low distortion: the 2270 is rated for 70W per channel into an 8 ohm load < 0.3% distortion; the FM section is very sensitive and selective, too.

This receiver came into the shop working “okay”. There was a lot of distortion in the FM, and overall it sounded muddy and a bit thin. The original capacitors were going south but fortunately nothing had catastrophically failed so it would clean up very nicely. I started off replacing the regulated power supply capacitors and adjusting the power supply. After each board repair I like to power it back on and verify each subsystem, so this made sure nothing would go wrong while doing the rest of the receiver. The board-mounted electrolytic capacitors were replaced with top of the line Nichicon Fine Gold audiophile capacitors; the chassis mount capacitors with slightly up-rated Kemet caps.

There’s only one cap on the phono pre-amp board:

Next, onto the tone board where I cleaned and lubricated all the controls:

The FM discriminator on this one had 6 more electrolytic capacitors, and an old school TO-5 style IC – actually the only IC in the entire unit.

The AM board in this receiver is mounted above the FM stereo demodulator.

Underneath, the stereo demultiplexer board got the same treatment:

This receiver had a major repair at some point in the past. One final board was original; one was from a much later 2270. Most likely something failed back in the ’70s and it was replaced under warranty.

Each final amplifier only has two electrolytic capacitors to replace:

Finally, it was time to check it all out! I started with adjusting the bias and DC offset to ensure the amplifiers would perform up to spec for the rest:

, then proceeded through the RF alignments:

The FM receiver was definitely out of spec. The dial alignment was correct but the distortion spec was very bad.

After 11 adjustments for FM, the distortion vanished:

I measured the power and distortion of the amplifier through the line input, too. This receiver was able to produce a bit over its rating, with 96W output at 0.25% THD. Not bad at all!

Ready to go!

This receiver is fantastic. It’s cleaned up perfectly and now it’s performing better than new. Should last for a long time, too!

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Use Copper Shielding Tape to Protect Dial Strings from Hot Tools [Tips and Tricks]

Dial strings are, quite frankly, about the worst things in the world. They’re usually a complex and finicky mechanical system parked right in the middle of an otherwise straightforward electrical project, and if a string breaks good luck getting it back together again in all but the simplest of dial string arrangements. And they break easily. On older, tube gear the dial strings have often worn out and snapped with age and friction. On newer gear, the dial strings have often been snagged on the case at some point during a previous repair attempt, or even worse, they were accidentally nicked with the soldering iron and burnt or melted apart.

That’s a problem which has happened to me quite a few times, even with a steady hand and the best of intentions. After spending many hours re-stringing the dial on a 1970 Toshiba tabletop transistor radio after my soldering iron caused it to snap where the string passed very near the amplifier PCB, I was inspired to come up with a solution that’s a bit more reliable than “just be more careful”: copper shielding tape!

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Copper shielding tape is an extremely important part of an electronics test bench. It’s very handy to shield a sensitive part of a circuit from electrical interference, but also, it can shield from thermal interference as well! In this case, because the copper foil is a thin piece of metal with a high melting point, the soldering iron brushing up against the foil won’t damage the string under it, and won’t heat it up nearly enough to cause damage to anything underneath for a short tap. This is the perfect solution to the problem of dial strings snapping when trying to solder too close to them. Copper shielding tape can be soldered, so it’s perfect to provide some protection against an errant soldering iron. A small 2″ section wrapped around itself with only a small section of the adhesive removed to form a cylinder was all it took.

Copper shielding tape is extremely useful to have around. It comes in a variety of styles, but I’d recommend one that’s about 2″ wide and has a conductive adhesive so it can act as a shield without soldering as long as it’s touching a metal chassis somewhere.

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I stock a full roll of 2″ x 55 Yards ($56.95) as I use this while repairing Bose equalizers and stereo receivers, but it comes in other sizes. A five-foot section ($15.95) might be a better choice if you don’t see yourself using it often, or if you’ll only use it as a soldering iron shield. It’s available in smaller, narrower sizes also: 1″ x 5′ ($10.99),  0.75″ x 18′ ($8.28), and 0.25″ x 18′ ($5.05) but these smaller and narrower sizes are really more appropriate for actually shielding seams, etc. than trying to protect a dial string.

If you try this out yourself, let me know how it goes!

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Toshiba 11H-540F Tabletop Transistor Radio Overhaul

I recently got to work on a little tabletop transistor radio from the late ’60s, maybe 1970 at the latest, from Toshiba: the 11H-540F. Not the catchiest name, but it was near the top of its model line-up featuring 11 transistors, AM and FM, and a line input. Audio power output about 1.4W into a 4 Ohm speaker.

It’s the transistor-age equivalent of a personal radio from the tube era. Solid middle of the road performance and a decently stylish package. Its owner was reporting that it wasn’t sounding that great, and she got an electric shock when hooking up an iPod to the back. It also had a lot of noise when first turned on, and the band switch was dirty and wouldn’t stay in one position. Basically it just wasn’t working well at this point.

I pulled the chassis out to get started. Definitely time for a rebuild. This 500 uF 6V capacitor had cracked and started leaking out the top.

The power supply board, with one pass transistor and a set of rectifier diodes. Replaced the 500 uF 15V capacitors with new 470 uF 16V models.

To work on the rest of the boards, the dial face has to come off:

In progress replacing components. I’d power up every few capacitors just to check, since these very early PCBs can develop cracked traces very easily. By checking regularly, I’d know if a trace broke with the last component I installed. Fortunately, none did!

Ultimately, everything ended up getting replaced.

A shot of control cleaner into the band switch and into the volume control cleaned up the scratchiness and intermittent connection. With all new caps, the static and noise on turn-on was completely gone, too.

It’s back to like new condition. No more shocks, no noise and crackling, no randomly cutting out and needing to fiddle with the switch. Just a warm vintage sound. This radio is rated for 1.4W max into its internal 4 Ohm speaker, and it managed this at around 2.5% THD. That’s after adjustment, but the nature of the distortion, the frequency response, and the speaker setup meant that it actually was still a pleasant sounding and non-fatiguing audio source. Perfect for background music in an office, for instance. It looks pretty sharp, too, with the atomic design above the dial and a nice wood cabinet and reddish grill cloth.

Here’s to many more years of happy listening!

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HP 143A Wide Screen Oscilloscope Mainframe Restoration – Part 2

Part 1

I’m continuing to work on getting my HP 143A ocsilloscope mainframe fixed up as a dual-trace X-Y display.

A lot of the time has been spent on reading and researching, but I’ve picked up an important tool that will help get me there: a Heathkit Oscilloscope calibrator.

This is a simple but important little device which will help me calibrate several of my oscilloscope projects. It produces a precise DC output level from 1 mV – 100V in multiples of 10, along with precise crystal-controlled frequencies for calibrating a timebase, etc This one was a kit, but it was put together well and is in great cosmetic shape for its age.

The heart of the calibrator is a 4.000 MHz crystal oscillator. This reference is passed through a series of frequency dividers and multipliers to obtain the calibrated reference frequencies.

I hooked it up to my scope to test. The frequencies were spot on with my scope’s internal counter (4-digit, so 1.000 MHz). I didn’t check against my more precise counter but this will certainly be good enough – I’m not an NIST cal lab (and don’t want to be!) so a “bench cal” will be just fine for these old scope repair projects.

All the functions check out. I’ll probably replace the 4 electrolytic capacitors as a preemptive measure just to ensure it doesn’t develop problems while I’m using it just to be sure. Otherwise, though, it’s going to be very useful for the 143A, and also my HP 130C oscilloscope project as well.

I’m still looking for another HP 1402A dual-trace amplifier, since this mainframe needs two identical amplifier modules to be used as an X-Y display. If you have one, please let me know!

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Harmony H500 Solid State Guitar Amplifier Repair

And now for something a little different, this time it’s a vintage guitar amplifier: the Harmony H500.

The owner sent it to the shop out of the cabinet to be serviced since it quit putting out any sound. It’s a pretty straightforward circuit with 3 transistors and a handful of passive components and tone controls to adjust the sound.

Harmony H500

Inside, it shows clear evidence of having been worked on before, and not quite up to standard. The caps were replaced with more or less random values of capacitance and voltage ratings; it was originally fitted with a 40 uF, 30 uF and 2 uF cap.

Since the capacitors on something this age always need to be replaced, that was the first step. Afterwards, though, no amplification on the input meant the transistors were dead. I replaced them with new 2N3391s and she fired right up.

This little amp delivers about 1.5W of power output from 8.2W at the wall. Not too bad!

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