I found a Samsung 225BW LCD sitting on top of my apartment’s dumpster, and figured I’d drag it upstairs. It’s a few year old model but it’s better than the current older Dell LCD that I’ve been using (1680×1050 versus 1440×900). A quick check showed that it would power on, sort-of, but the power light would flicker constantly and there was no backlight.
I popped it open, suspecting a problem in the power supply – and turns out that was right. Several capacitors on the board were showing signs of failure. Capacitors are the main component I replace in the vintage radios but cost-cutting OEMs are often known to use caps that fail after only a few years when new to save a few cents on each part that goes out the door on new things as well. In this case their 330uF and 820uF @ 25V caps had failed and the logic board was no longer getting good power.
Modern electrolytic caps fail by bulging and leaking out the top and/or the bottom, it’s easy to see at a glance. The top two are bulging and leaking; the bottom ones are bulging only which is a bit difficult to make out in the photo.
This project is one of the reasons I bought a Hakko 472D desoldering tool. It’s made for reworking through-hole and point-to-point boards, and works by melting the solder and then applying a strong vacuum through the center of the nozzle sucking it out of the way and cleaning the connection. It wasn’t cheap, but I thought it’d be important to have one of these as I do more types of electronics hobby work. I tested it out on an antique radio and it works perfectly for the annoying old joints.
This board is pretty easy to work on, the components are widely spaced and marked.
Even though it’s not bad, I’m replacing the large main filter as well – just in case. It’s the same brand as the failed ones.
Here I’ve depopulated the bad components from the board and have placed the main filter back in position, with the old one above it for comparison.
The new caps are larger than the old ones – for the same ratings, a larger size capacitor is going to be a bit more durable. For example these 330uF 25V models:
Slid the components through the top, spread the leads to hold them in position while soldering and reattaching:
Bad planning on my part meant I forgot to take a photo of the board post-repair, but it only took about 30 minutes to do the entire thing – most of which was spent figuring out how to adjust the Hakko. And for the power-up:
Success! Back to life. This LCD goes for around $150 online even today and I’ve been meaning to add a second monitor to my desk anyway, so I’m about 1/3 of the way to recovering the cost of that desoldering station after the first project. One down, two to go….This project required 3x330uF 25V capacitors, 2x820uF 25V capacitors and 1x150uF 450V capacitor which came out to $9.83.
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I’ve got 6 of these monitors from my work. They all started “breaking” one by one, despite the fact that I told them it’s an easy fix, they just kept throwing them in the graveyard to be recycled. They replaced them with newer 24″ LCDs. I bought a batch of capacitors and just waited for these things to “die” now I got a bunch of them
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